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April 11, 2006
Dear Mak, This morning the Whelp was put back into the water and
she is back in her berth at the Catamaran Marina. When I arrived
Thursday America was busy sanding the boat. AS you read this description
consider four people sanding and varnishing away like mad as sort
of the rhythm of the experience. It was useful because there was
always some one here to lend a hand.
I took the taxi directly to the yard to inspect the blocking plan
and see what Level of competence I was dealing with. I was immediately
pleased with Dion Hector and his crew. We scheduled a 7AM arrival
for hauling and the intention of going off of the ways Tuesday morning.
I went back to the boat and with out unpacking started to put the
intermediate bearing in. The wood block was 1/8 too high so I had
a long rubbing session on the dock to wear down the extra wood.
After two sessions it was getting close AND THEN the wood split
at the glue line. I was all done sanding luckily it was close enough
to make fit by removing the two washers under the flexible mounting
bock. I greased it up and ran the engine ahead at 1000RPM for about
a half hour. The bearing got hot, 170 deg, so I loosened the hold
down bolts and the upper half and the temperature dropped. It was
running at 105 degrees when I called it quits at 11:45 PM.
I was up at 5:30 the Friday morning dropping the inflatable into
the water and bringing the second anchor rode over to the dock so
we could leave it for John to haul out and clean off. 6:30 departure
brought us to English harbor at 7:05 and we hung out waiting for
the ways to be lowered. It started down at about 7:30 and we were
out of the water very smoothly by 8:00.
Looking the hull before pressure washing it was quite clean. We
had discoloration around the SSB ground in a circle about 4 feet
in diameter. There was also a nasty looking separation of the glass
down at the bottom of the keel. it was about 4 feet long on the
port side we determined that the really ugly part was the Kevlar
coming unglued from the hull ad the crack was mostly in the outer
layers and didn't really involve the wood underneath.....so we had
this ground down and turned out attention to the crack in the glass
covering layer in the boot top at the stem. It turns out that this
was a bubble in the original glass work and it could be quickly
dealt with. This was the major reason that I planned to haul in
Antigua rather than Maine later on so it was a relief that the crack
wasn't because of a continuing problem with water penetration into
the stem. Shower and out to diner.
Saturday saw the yard crew back sanding and painting the first
bottom coat on the hull. I started unpacking the gear I brought
down with me. NO air conditioning because we were on the ways no
refrigeration, not a breath of air I would unpack an item and then
stow it or install it. And escape up to the deck. At noon I escaped
and walked to the Antigua marina to get the cell phone up and running.
Also went to the Yacht club and signed up for the Classic Regatta.
I was all in by 6:30 and really didn't make much progress since
nothing I installed wanted to behave. The InterPhase showed no sign
of life and the Inmarsat -C needed me to go up to the top if the
mast to install the antenna and America was busy varnishing. When
I was installing the Inmarsat -C I noticed that the Noland Nmea
183 splitter wasn't working. The list of things that weren't working
was growing not shrinking. Aft Head holding tank pump out. Aft Grey
water stuck float switch. Main engine tack shuts of when the generator
runs. Computer giving one device fails to function at start up warning.
Computer printer not working. I called it quits took a shower and
went out to dinner. Had a salad. When I returned to the boat the
mosquitoes were out with a vengeance. Little tiny mosquitoes.
Sunday America was back at 8:00 and the yard subcontracted with
Woodstock crew to do the glass work Nice guys, Phil doing the glass
work and Danny lubricating the thru hulls he got all but the port
cockpit thru hull simply because he couldn't fit to get access.
The high point of the day was that America took me out to lunch
with his crew at a local eatery, Good but strange food. I had curried
goat. I spent some time at the dock yard at an internet cafe tracking
down Noland engineering so I 'd have a phone number Monday morning.
Dinner was a pizza . and back to the Mosquitoes. I actually got
out the water colors book and did the first exercise.
Monday America was at it bright and early. I hadn't gotten a lot
of sleep because of the formations of mosquitoes dive bombing me.
I went to English Harbor and had scrambled eggs for breakfast. I
made contact with Noland engineering and they are going to send
a new unit under warranty. I called a computer guy and he took the
printer away and promised to come back to the Cat club on Tuesday
morning with a report on the printer and to get into the nitty gritty
of the WIFI and other stuff. I made two trips to Antigua Sails to
replace the lower batten we lost coming down from Bermuda. Bought
yellow paint and marked the anchor chain. Cleaned the speedo thru
hull and paddle and sanded the shells off of the depth sounders.
Fueled up the dingy and had a steak and two beers before consigning
my self to the mosquitoes. This time I put all of the hatch screens
up and had a tolerable but sweaty night.
0700 Tuesday morning I was inspecting the boat and found the paint
job on the boot top at the stem was awful. Out side of that every
thing else was acceptable. The boat went back in t 8:30 and we steamed
around to the Cat CLUB. America handled the anchor and chain. The
mooring was acceptable for a green crew. At 1030 the computer guy
came back and pronounced the printer dead. He also connected me
up to the WIFI and will be back tomorrow to investigate the device
that isn't working. America is varnishing like crazy so I am in
the way. I took the zodiac around to English Harbor to square up
with the Yard and send the bill to Joanna. On the way back I stopped
at the Antigua Marina and picked up a steak for dinner the first
time I will have cooked for my self on this trip. I squared away
with John Nobbs for babysitting the boat,(Paid his Catamaran marina
bill with the Visa Card $820 more or less ) found out who can make
food for us to freeze for the trip north.
A steak, the Ice box is back on , the air conditioner is working
Jazz is playing on the stereo...I found my paisley handled screw
driver... all is momentarily right with the world.
Tomorrow I think that we will be getting more organized and settled
in.
That is what is going on here.
Cheers Phin
April 26, 2006
David, Mak, Hope that all is well with you. Lions Whelp is about
388.7 miles from Bermuda motor sailing at 8.5 knots in a delicious
high. I'd be sailing at 4 knots except for the frontal passage that
is due in Bermuda at 1400 EST on the 28th. I seem to get in about
two hours before frontal passage the last two times.... and have
a fun, wild, wet ride from St Georges to Hamilton.....as opposed
to slogging the last 30 miles to windward.
I am firming up the window for the sail from Bermuda to Portland.
I have to be in Portland BY the 2nd of June. Because we are hosting
Bruce Schwab and Ocean Planet at PYS that weekend. If I back that
up five days the latest we can leave comfortably is Saturday the
28th.
Since I am looking for a high to cross the Gulf stream on I fudge
72 hrs for a weather window which means the boat is ready to go
and on standby from the 25th. I'll be on the boat on the 22nd- 23rd
to check out systems. You are welcome to arrive any time before
clearing. ( Abbott arrived in a taxi while we were at the customs
dock last year.) Hey it works for me!
The magic passage planning number is 168 miles per day so the trip
should take 4.5 days. If it is flat ass calm we can power the whole
way in 4 days.
Can you pass this on to Teddy. Looks like the crew is Phin, Abbott,
David, Teddy, Some one from Tabor and we'll see. we're sailing up
from Antigua with four and it has been acceptable but busy because
of the watches.
Cheers! Phin
April 29, 2006
Been a busy Day. Powering now. C 348 M Trying to get westing for
a date with a front tomorrow evening. The wind has been fluky and
we have been rolling around pretty heavily. At 10:00 I heard a huge
crash. the guys had rigged a preventer through a turning block to
the Port cockpit winch and the boom crashing over had pulled the
winch right up from the deck. The two aft bolts in the pedestal
were 1.25 inches long and just screwed into a g-10 sleeve. The four
forward bolts were thru bolted to washers of various descriptions
the one with no washer just pulled up into the headliner. The g-10
sleeve broke where the bolt ended and two pieces of the deck split
out with them.
Squalls coming down around us we managed to disassemble the winch
and pedestal, find some more G-10 tube tap that for the 1/4 inch
bolts, make longer bolts, glue down the teak, drill out the old
G-10 re bed and install the pedestal just as the first unavoidable
squall hit. Water was pouring down the bolt holes into my face and
into my bunk as Jim Cram on deck tightened the last bolts and started
to squeeze out the 5200 bedding compound. Had the repair finished
and the winch back in service by 1300. #1 the shock loads are astounding.
#2 the rope used had absolutely no stretch. #3 Screwing into g-10
tubes us insufficient faced with this violent loading. The reason
for the G10 tubes was because of the unfortunate location of the
winch over a bulkhead. In Maine we will have to move the winch forward
and get some decent blocking in place.
I am trying to download the grib files to check on the front we
should see Sunday night and another Monday night. There are squalls
all around us with impressive lightening. It is a good thing to
have the boat water tight again and the winch operating.
Cheers! Phin
May 1, 2006
Hi there. Sent an e-mail to Mak about winch repair hope he passed
it around. Noon position 24 07'N 64 34W.Wind 270 deg 15 knots Speed
7.8 kn COG 359M Blue skies with thunderheads building. Almost half
way. I was routed way west so that when the low moves away from
Bermuda we can ride the westerlies in. Right now we are close hauled
in about 6 foot seas. A little on our ear. The weather is good and
if we can stay tucked in under the low as it moves off then we will
not slip into the lighter air that is working in behind us. I would
almost like for it to stall and dissipate so we have the benefit
of the favorable winds and they do not go too much into the NW.
It is still too soon to predict the Bermuda ETA. Could be as early
as Thurs noon if we can hold the wind.
The crew is great I am being well fed. Pierre had a visible panic
attack when he realized that the coffee in the cabinet was decaf.
The look of terror didn't end until he found the stash of Maxwell
house in the Main cabin. However, I am constantly reminded that
the actual Schooner experience is lacking even though they are good
sailors and are picking up things quickly.
Had a hard time starting the generator this morning. I don't think
it likes being on it's ear. Out side of that all things are nominal.
Cheers! Phin
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